Which came first?
Originally Posted by jimknapp,Nov 17 2007, 07:51 PM
Racer,
I agree it is worthless (almost) without pics. How can I post them to an S2KI message?
Jim
I agree it is worthless (almost) without pics. How can I post them to an S2KI message?
Jim
AT LAST!
Okay, here are some pics of the destruction
http://i218.photobucket.com/albums/cc98/ji...pp/IMG_0803.jpg
http://i218.photobucket.com/albums/cc98/ji...pp/IMG_0801.jpg
http://i218.photobucket.com/albums/cc98/ji...pp/IMG_0799.jpg
Hope this works. This is a test of sorts.
All the best,
Jim knapp
Okay, here are some pics of the destruction
http://i218.photobucket.com/albums/cc98/ji...pp/IMG_0803.jpg
http://i218.photobucket.com/albums/cc98/ji...pp/IMG_0801.jpg
http://i218.photobucket.com/albums/cc98/ji...pp/IMG_0799.jpg
Hope this works. This is a test of sorts.
All the best,
Jim knapp
Hey, I even figured out how to upload the pre-destructo dyno results!
http://i218.photobucket.com/albums/cc98/ji...destruction.jpg
Notice how far off the Air/Fuel ratios were for most of the first two runs.
If you look carefully you'll see the third run, the purple one, was our first pass with some fuel corrections and we'd already added 7 - 8 HP. Then the Air/Fuel probe blew out of the tail pipe and the reading went straight up, and about 8500 the party was over.
Oh well.....
Keep the $hiny $ide up,
Jim
http://i218.photobucket.com/albums/cc98/ji...destruction.jpg
Notice how far off the Air/Fuel ratios were for most of the first two runs.
If you look carefully you'll see the third run, the purple one, was our first pass with some fuel corrections and we'd already added 7 - 8 HP. Then the Air/Fuel probe blew out of the tail pipe and the reading went straight up, and about 8500 the party was over.
Oh well.....
Keep the $hiny $ide up,
Jim
Here vvvv ...

If I am reading this right, it looks to me like the A/F shot completely off the chart at around 7,100 RPM. If that wasn't due to the A/F sensor blowing out the tail pipe, then the extremely lean condition may have somehow been a factor, perhaps (???) due to heavy detonation???
Not trying to second guess you, but why didn't you abort the pull when the A/F spiked?

If I am reading this right, it looks to me like the A/F shot completely off the chart at around 7,100 RPM. If that wasn't due to the A/F sensor blowing out the tail pipe, then the extremely lean condition may have somehow been a factor, perhaps (???) due to heavy detonation???
Not trying to second guess you, but why didn't you abort the pull when the A/F spiked?






